Investigation of the zinc re-grinding circuit at Boliden Garpenberg

University essay from Luleå tekniska universitet/Institutionen för samhällsbyggnad och naturresurser

Author: Nils Merum; [2021]

Keywords: Flotation; re-grinding; Garpenberg; Boliden;

Abstract: Boliden’s mineral processing plant in Garpenberg wanted to investigate their zinc-regrinding circuit. The re-grinding circuit had performed subpar when running as the total recovery of zinc was lowered and problem with the dewatering of the final concentrates was also noted. Therefore, the zinc re-grinding circuit is currently not being used. Furthermore, it was noted during investigations about silicate depressant that the zinc circuit had problems with coarse sized sphalerite particles locked with silica. Which could perhaps be liberated with the re-grinding circuit. The purpose was therefore to investigate how a re-grinding step could be used to liberate locked sphalerite particles from gangue. The practical part of the thesis involved lab-scale SMD-mill, re-grinding of the scavenger concentrate and cleaner tailings which are the two streams being fed to the SMD-mill in the plant. The re-grind was done in three fractions: bulk, +90µm and +125 µm fraction with subsequent lab-scale flotation afterwards to identify how the re-grinding effected the flotation results. Also, a small QEMSCAN analysis was performed for the +90 µm fraction to identify how liberation was improved by re-grinding. The flotation trials were performed with two references and two different intensities for the re-grinds.  The results showed an overall increase in grade of zinc in the concentrate with increased grinding for all the trials. SiO2 and MgO content (typical elements for silicate gangue) was also reduced in the zinc concentrate, showing that re-grinding helped liberate locked sphalerite particles. The QEMSCAN results showed that the liberation of sphalerite particles in the +90 µm fractions increased with re-grinding. For the bulk fraction scavenger concentrate the zinc recovery increased slightly, for the +90 µm fraction scavenger concentrate, a slight decrease in zinc recovery could be seen after re-grinding. The decrease in recovery was larger for the cleaner tailings (bulk and +90 µm) and was decreased further with increased grinding. However, for the +125 µm fraction tests, zinc recovery was increased for both scavenger concentrate and cleaner tailing. The references showed an overall high recovery but a zinc grade in the concentrate close to the feed grade of zinc and contained a high grade of SiO2. Indicating that without re-grinding the amount of free sphalerite is low. Overall, the re-grind and flotation tests pointed towards that value can be created for the plant by re-grinding the scavenger concentrate and cleaner tailing. 

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